Notice ID: | 290 |
Notice Type: | MAJ |
Critical: | Y |
Notice Status Description: | |
Reqrd Rsp Desc: | |
Posting Date/Time: | 2014-12-19 07:43:45.0 |
Subject: | Stingray Leak - Update 8: Repaired |
Notice Effective Date/Time: | 2014-12-19 16:00:00.0 |
Notice End Date/Time: | 2200-01-01 00:00:00.0 |
Notice Text: |
The leak located on Stingray’s 24” Pipeline segment 8920 have been repaired.
The following platforms have been cleared to resume production:
Garden Banks 189 Chevron (PIN 400189) Garden Banks 668 Gunnison (PIN 400668) HI-A330 HIOS/Stingray (PIN 70A330) West Cameron 544 Arena Offshore (PIN 600544) West Cameron 548 Arena Offshore (PIN 600548) West Cameron 552 Black Elk (PIN 600552) West Cameron 661 Tarpon (PIN 600661)
For the above mention locations, effective with the ID 2 Cycle for gas day Friday, December 19, 2014 (9:00 PM CCT), the Force Majeure issued on December 14, 2014 (see Notice ID 288), pursuant to Section 23 of the General Terms and Conditions of Stingray’s FERC Gas Tariff, is no longer in effect.
The following platform continues to be required to remain shut in until further notice:
West Cameron 616 W&T Offshore (PIN 600616)
For West Cameron 616 W&T Offshore (PIN 600616) ONLY, the Force Majeure issued on October 5, 2014 (see Notice ID 265), pursuant to Section 23 of the General Terms and Conditions of Stingray’s FERC Gas Tariff, remains in effect.
As a reminder, upon return to service, Stingray expects all platforms affected by this outage, especially those with pipeline imbalances, to work with Stingray to schedule makeup.
For questions concerning this notice, please contact Transportation Services at (713) 457-8990.
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